1. Introduction
The dissolved gas analysis (DGA) is the most widely used method in the diagnosis of power transformers. There are many publications confirming the usefulness of this method as well as its effectiveness, as for instance in [
1,
2,
3,
4,
5,
6,
7]. The works mentioned showed that with the application of the DGA method, it is possible to detect a thermal or electrical defect of the transformer’s insulation system at a stage that will prevent the final damage of the unit. However, in the case of bushings with the oil-paper insulation (OIP), the basic method of cyclical diagnosis according to [
8] and based on the service experience, is the measurement of capacitance C and dielectric dissipation factor (tanδ), then the infrared scanning, and finally DGA. A limitation of the use of the DGA method lies in the need to respect the special procedures of taking the oil sample from the bushing, which, without a special commitment, may cause the bushings damage and the necessity of the transformer to be switched off. Hence, the literature data on applying the DGA method in the bushings diagnosis are very limited [
9,
10,
11,
12,
13]. In [
9], Malpure et al. analyzed the results of the DGA of bushings of three transformer units. The authors considered DGA as a supporting tool for typically used diagnostic methods based on capacitance and tanδ measurements of bushings. In all cases, the data concerning DGA indicated the occurrence of partial discharges (PDs) in bushings which were confirmed by on-site PD tests. The authors’ conclusion was that the DGA supplemented by electrical tests may be significantly helped in the diagnosis of bushings when electrical tests did not give unambiguous results. In turn, Mohseni et al. [
10] proposed a precise simulation as well as practical analyses demonstrating the impact of bushing faults on the frequency response analysis (FRA) signature of the transformer and connected the simulation results with a real object—132 kV power transformer, for which the FRA results were set with the results of DGA. The conclusions found by the authors were that the bushing faults have an impact on the FRA signature and DGA and both methods may supplement the classical approach based on C and tanδ. In [
11], the authors described the case studies of the series of OIP bushings, in which gas concentrations were measured and DGA analyses were done as additional methods supporting the above mentioned conventional methods and dielectric frequency response (DFR), which was also applied as a diagnostic tool in the assessment of the bushings condition. The general conclusions were that DGA may strengthen the diagnosis elaborated on the basis of more conventional methods, however, with a lower level of success than DFR. In [
12], the fault diagnosis and tear-down analysis of five 500 kV OIP transformer bushings were presented. In the authors’ considerations, next to the capacitance and tanδ measurements, the frequency domain spectroscopy (FDS) method in combination with DGA as a supplementary field diagnostic test were applied. The tests performed indicated the effectiveness of adopting FDS in combination with DGA. In particular, this effectiveness was visible when the partial discharge-based defect took place. In the work of Ensico et al. [
13], DGA was also used as the supporting method in the diagnosis of six high voltage bushings, which were removed preventively from the service. Next to the capacitance and tanδ measurements, the other laboratory techniques as a partial discharge measurement and DFR were applied together with DGA. The authors found that DGA based the diagnosis indicated with a success activity of partial discharges, which confirmed the data from other laboratory measurements. In the case of other literature reports, DGA was noticed as a useful diagnostic tool for the assessment of the bushings condition.
The general rules concerning the detection and characterization of faults in bushings, using the dissolved gas analysis, are the same as in the case of power transformers. This means that in the first step of the condition assessment of bushings it is necessary to check whether the measured gas concentrations exceed the typical values, and if this takes place, the nature of the defect can be determined in the next step.
According to the IEC 60599 Standard [
14], the data presented in
Table 1 are proposed to be considered as typical values.
In turn, on the local market, the typical values of gas concentrations in bushings are proposed to be accepted according to the regulations [
15], as presented in
Table 2. In the case of carbon monoxide and ethylene, they are a bit more restrictive than those proposed in [
14].
However, CIGRE, in brochure no. 771 [
16], presented 95% of typical gas concentrations determined on the basis of data collected from surveys carried out in several European countries. These data take into account the nominal voltage or construction of the bushings. The values proposed are significantly higher than these from the IEC 60599 Standard. The graphical representation of these data based on [
16] are shown in
Figure 1.
There are five typical kinds of faults detected in the case of bushings. They are set in
Table 3 together with the causes of these faults and the corresponding characteristic gases dissolved in oil.
According to [
14], knowing the values of the concentrations of gases dissolved in the oil, the nature of the fault can be recognized on the basis of a simplified analysis of the following values of characteristic ratios: C
2H
2/C
2H
4, CH
4/H
2, C
2H
4/C
2H
6, CO
2/CO. The criteria used in this field are presented in
Table 4.
In this case, when a more precise diagnosis is needed or when more than one fault is indicated, the relationships accepted for power transformers should be applied, as presented in
Table 5.
In a number of cases, ratio methods, including the one recommended in the IEC 60559 Standard, cannot identify the nature of a potential fault for the measured gas concentrations. In such a case, it is recommended to use the well-known and widely used method of Duval’s triangle in the basic version (version 1) [
18,
19], which is used not only in the diagnostics of power transformers, but also in the case of bushings.
Based on the above considerations, the authors decided to present further in this paper a case study when the voltage collapse during the lightning impulse tests of new power transformers was noticed and when the repeated tests finished with a positive result. The step-by-step process of reaching the conclusion on the source of the failed test, which was found in the bushings, was presented based on DGA as a key method of the investigations.
2. Case Study
During the tests of 115/16.5 kV, 16MVA, YNd11 power transformer by a negative standard lightning impulse voltage (1.2 µs ± 30%/50 µs ± 20%) of peak voltage equal to 550 kV, the voltage collapsed on the voltage waveform tail when phase 1U was tested. The transformer manufacturer as well as the buyer agreed to repeat the test, and this time it finished with success. A confirmation of the negative and positive lightning test of phase 1U is shown in
Figure 2, where the course registered during the failed test is presented in
Figure 2a and the course registered during the repeated test is presented in
Figure 2b, respectively. Herein, it is important to point out that the other phases passed the lightning test positively. Therefore, the courses corresponding to these phases were similar to the course presented in
Figure 2b.
Despite the positive result of the second attempt, it was decided to conduct a study to find the cause of the failure of the first test on the 1U phase. The scope of the investigation included:
- (1)
Checking the testing setup;
- (2)
Analysis of the transformer construction;
- (3)
Analysis of technology of the transformer manufacturing;
- (4)
Tests and external inspection of the transformer.
The investigation performed did not show any inaccuracies in the testing setup as well as any abnormalities at the lightning test conducted. However, it confirmed the correctness of the design process and of all the steps in the process of manufacturing, including drying of cellulose insulation, filling the transformer with oil, and the impregnation process. Additionally, the oil sample was taken from the transformer in order to determine the concentrations of gases dissolved in oil. The results in this field together with data from the measurements performed before the lightning tests are quoted in
Table 6.
As we can see from the table, the analysis of the measured gas concentrations did not indicate any problems. Hence, in addition, the HV bushing of the 115 kV side of the phase, in which the voltage collapsed during the lightning test (phase 1U), was tested. The dielectric dissipation factor tgδ and the insulator capacity were measured and, which is not a common practice, an oil sample was taken from the considered bushing to determine the concentration of gases dissolved in it. The results concerning tgδ and capacity, as well as the gas concentration measurements were presented in
Table 7 and 8, respectively.
As it is clearly seen in the quoted table, the results concerning tgδ and capacity did not indicate that the bushing considered might be damaged. Additionally, the measured value of the oil moisture (6.6 ppm) did not indicate on its potential contribution to the causes of the phenomena observed during the lightning impulse tests.
The content analysis of
Table 8 shows an exceedance of the typical values given by the IEC 60599 Standard by hydrogen, methane, ethylene, and acetylene. Additionally, the mentioned gases exceed the typical values used locally in Poland [
15]. Therefore, the values from
Table 8 indicate that the cause of voltage collapse during the lightning test of the power transformer could be due to the defect of the bushing. A simplified analysis of the values of the characteristic ratios in accordance with the guidelines of the IEC 60599 Standard (C
2H
2/C
2H
4 = 753/791 = 0.95; CH
4/H
2 = 672/965 = 0.70; C
2H
4/C
2H
6 = 791/67 = 11.24; CO
2/CO = 1769/141 = 12.55) was indicated on the thermal fault. However, a very high concentration of acetylene and simultaneously the value of C
2H
2/C
2H
4 ratio close to 1 might also indicate the discharges as a potential cause of the voltage collapse during the lightning tests. Additionally, applying a full version of the ratio method recommended by the IEC 60599 Standard clearly identified the discharges of high energy (D2) in the bushing considered, which is confirmed by the data in
Table 9.
Similarly, the analysis made using the basic form of Duval’s triangle indicated the high energy discharges (D2) in the bushing. The results in this field are presented in
Figure 3.
Taking into account the conclusion from the quoted analyses and the lack of visible effects of discharges, the disassembly of the bushing was made and its internal inspection was ordered. On its basis, the discharge occurrence was confirmed—the arcing developed along the inner surface of the epoxy insulator from the tube to the flange at ground potential, as shown in
Figure 4.
Considering different options of the noticed situation, it was assumed that the direct cause of the discharge formation was an air bubble present in the lower part of the bushing. It was created as a result of an incorrect way of transporting the bushing and its storage. This assumption was confirmed by the noticed way of arranging the bushing in the transport crate, as shown in
Figure 5. The photograph from this figure also shows a badly placed information label. The bushing, after placing in the transport crate, should have an oil level indicator downward, towards the bottom of the crate and the information label on the bushing head should be placed on the opposite side of the indicator.
The source of the agglomerated air could also be an excessive fit of the capacitor part of the bushing inside the housing (
Figure 6). As a result, after filling the bushing with oil, the air could not be released.
The relative dielectric permittivity of gas (εgas ≈ 1) in the bubble is more than twice lower than that of oil (εoil ≈ 2.2), which results in the presence of proportionally higher values of the electric field stress (simply Egas = Eoil · εoil/εgas) and significantly facilitates the formation and development of discharges. After the occurrence of discharge during the first lightning impulse test, the air bubble disappeared and the strength of the insulation system intended by the designer was achieved, which resulted in the successful completion of the repeated test.
An identical situation, as described above, happened for four more transformers equipped with the same types of bushings. Similarly, as in the case mentioned above, only the bushings of the selected phases did not pass the first lightning test.
Table 10 summarizes the values of the measured gas concentrations from the bushings installed in these transformer phases, in which the voltage collapsed during the lightning test.
When analyzing
Table 10, it can be noticed that in all cases the concentration of methane, ethylene, and acetylene exceeded the typical values recommended by the IEC 60599 Standard. In some cases, the typical values of hydrogen and ethane concentrations were also exceeded. The use of the full version of the ratio method clearly indicated the occurrence of high-energy discharges (D2) only in case 4. However, taking into account the obtained ratio values, as shown in
Table 11, it is reasonable to suppose that in other cases the discharge also occurred.
In turn, when using Duval’s triangle for the analysis of the gas concentrations in all cases, the discharges of high energies were confirmed, as shown in
Figure 7.