1. Introduction
In Italy, pellet stoves and boilers are popular residential heating appliances for several reasons, including state and regional incentives for renewable energy heating systems. Moreover, the cost of wood pellets is attractive as compared to other traditional fuels such as liquid petroleum gas and heating oil, which are common options in areas not serviced by natural gas. Finally, wood pellets are easy to store and use. On the other hand, the combustion of wood is a source of unhealthy emissions; this is particularly important in Northern Italy, where geography and average meteorological conditions hinder the dispersion of pollutants into the atmosphere. Products of combustion can be subdivided into classes according to several criteria. For example, one can distinguish between gaseous and solid emissions, or between emissions from complete or incomplete combustion. Considerable attention is generally paid to carbon monoxide (CO) emission; indeed, it is a sign of incomplete combustion and can be considered a tracer of other pollutants such as hydrocarbons or soot (that is, the organic portion of the total suspended particles). In addition to CO emission, an important parameter related to air pollution is particulate matter (PM), which identifies any particles released from the chimney. In recent years, nitrogen oxides (NO
) emissions from wood-burning appliances have been receiving growing attention, too. In combustion, three types of NO
with different formation mechanisms are known: thermal NO
, prompt NO
and fuel NO
[
1]. NO
is the sum of nitric oxide NO and nitrogen dioxide NO
, but NO is the only one present in a significant amount in pellet stove flue gas [
1]. It is well known that the principal mechanism of formation of NO
in biomass combustion systems is the fuel-NO mechanism, by which NO forms from the oxidation of the nitrogen in the fuel; on the other hand, the contributions of thermal NO
and prompt-NO
mechanisms are negligible for the relatively low temperatures reached in biomass combustion.
The insalubrity of carbon-based solid fuel combustion and its potential danger to health are extensively addressed in the literature. The scientific community in the field is looking for new methods for the reduction of these emissions, focusing on the causes of their generation to develop primary and secondary reduction measures. In this respect, fuel composition is a key aspect to consider. For instance, inorganic materials in the fuel are sources of emissions of solid particles, whereas the volatility of the elements contained in the fuel determines the amount of total suspended particles in the flue gases as found by Wiinikka et al. [
2] and Fuller et al. [
3]. Sommersacher et al. [
4] described how the amount of the volatile elements potassium, sodium, zinc, lead, chlorine and sulfur in the biomass can be used to predict the concentration of total suspended particles emitted during the combustion. Exploiting the fact that the main process of generation of inorganic suspended particles is the vaporization of inorganic compounds, some researchers have correlated fuel bed temperature with the vaporization of inorganic compounds and, therefore, with the generation of fly ashes (see, for example, the experimental works by Wiinikka and Gebart [
5] and Obernberger et al. [
6]). Indeed, as fuel bed temperature increases, larger quantities of inorganic compounds vaporize and, in turn, larger quantities of inorganic fly ashes are released. In best quality pellet A1 according to the ISO 17225-2:2021 standard, the ash content is low; the ash deposits are mainly composed of low melting temperature compounds such as K
SO
, KCl, Na
SO
and CaCl
and they tend to increase with CO content in the flue gases as fuel bed temperature increases [
7,
8].
In addition to fuel properties, burner pot geometry, burning power, air inlet positions, air staging, and excess air also influence emissions and performances of solid fuel combustion. As concerns burner pot geometry, differences in dimensions, air inlet positions, air inlet ratios and depth can lead to important variations in CO and PM emissions [
9]. For each stove, there is a specific range of burning power that optimizes combustion, as demonstrated by several studies—see, for example, the works by Morán et al. [
10], Colom-Díaz et al. [
11] and Fernandes et al. [
12], in which the same appliance was tested at different burning powers and an optimum interval was identified for the minimization of CO emission and fly ashes. Air inlet positions also influence emissions: Bunner et al. [
13] and Khodaei et al. [
14] focused on air supply strategies to reduce fly ashes generation. They found that the best experimental solution consists in reducing primary air, which directly invests the fuel, up to under-stoichiometric values, and increasing the amount of secondary air that invests the flame. Indeed, a lower amount of primary air reduces the temperature and velocity of combustion air in the fuel bed, as found by Caposciutti et al. [
15]. Measurements by Jancauskas and Buinevicius [
16] demonstrated that the temperature in the primary combustion zone decreases with flue gas recirculation, just above the fuel bed. In the work by Archan et al. [
17], the use of flue gas recirculation was found to diminish the average temperature due to the lower oxygen partial pressure and higher inert gas content, avoiding the formation of slag on the grate. As a result of temperature reduction, the entrainment of solid particles and the vaporization of inorganic compounds are also reduced. Instead, secondary air reacts with all products of incomplete combustion generated in the primary zone, such as CO, total hydrocarbons (THCs), volatile organic compounds (VOCs) and soot, completing all reactions and reducing products of incomplete combustion and fly ashes. Excess air, indicated by the oxygen (O
) content in the flue gases, strongly influences emissions, as shown, for example, by Petrocelli et al. [
18], Sher et al. [
19] and Moron and Rybak [
20]. In particular, an optimum excess air level in the flue gases exists that minimizes CO emissions, and its value changes depending on the design of the stove. Other studies have focused on flue gas temperature and the resulting temperature at chimney-roof penetration [
21,
22]. In some special conditions, such as during soot fires in the chimney, flue gas temperatures can reach peaks of 1200 °C, causing a strong reduction in efficiency and problems of safety [
23,
24].
In parallel with academic studies, international, national and local regulations on wood burning appliance emissions are becoming more and more severe. An example is the Ecodesign Directive, implemented by Commission Regulation (EU) 2015/1185 [
25], whose requirements for domestic biomass appliances came into force on 1 January 2022 (
Table 1). In some regions of Northern Italy, emission limits are even more stringent. From 1 January 2020, in Lombardy only the installation of “4 stars” and “5 stars” biomass-burning appliances is permitted, according to the classification of the Italian Ministerial Decree (DM) 186/2017 [
26] taking into account emissions (CO, NO
, PM and THCs) and efficiency. New limits on installation, replacement and incentives are constantly being introduced on a national and local basis. The NO
reduction has become more important in recent years after the introduction in Italy of the above-mentioned DM 186/2017, in which the top class, i.e., “5 stars”, requires that for pellet stoves the NO
must not exceed 100 mg/Nm
(13%O
) (
Table 1). Comparing this value with the figures reported in the literature, it is clear that respecting such limits remains a challenge, even with the best available technologies [
27]. Many recent works analyzed primary measures for NO
reduction. Air staging and flue gas recirculation are some of the possible solutions, which proved to be effective also in the reduction of other pollutants (see, for instance, the recent papers by Archan and co-workers [
27,
28]).
The recirculation of flue gas (FGR) is a technique of combustion optimization based on mixing combustion air with a fraction of flue gases to reduce the amount of O
in the combustive agents below 21% of O
. This entails a reduction of the fuel bed temperature and, consequently, a reduction of emissions. Early examples of FGR applications can be found in Liuzzo et al. [
29] and in Duan et al. [
30], where it was tested in a waste incineration appliance and in a pilot-scale vortexing fluidized-bed combustor fed with peanut shell, respectively. This technology has been tested with several fuels such as coal, waste, pellet, diesel and methane: Sung et al. [
31] applied it to a circulating fluidized bed facility with pellets used as an auxiliary fuel, Tu et al. [
32] to a grate firing boiler, and Shi et al. [
33] to small methane-air premixed-flame burner.
Considering studies on wood pellet or biomass-fired, fixed-bed combustors–the only possible configuration in domestic pellet stoves—in the early work by Morán et al. [
10], a reduction in NO
emissions was observed in wood pellets combustion with a strong FGR. In the tests carried out by Jancauskas and Buinevicius [
16] on an experimental small-scale model (20 kW) of an industrial biofuel boiler fired by sunflower seed hulls, increasing the FGR ratio in the primary air reduced NO
by about 20%. Good results in terms of NO
emissions—below the threshold of 100 mg/Nm
(13%O
)—have been reported by Archan et al. [
27] for a 200 kW multi-fuel biomass boiler and by Chen et al. [
34] for a 500 kW biomass boiler. A case with power size comparable to that of pellet stoves is the study by Zandeckis et al. [
35], who recorded a 11% reduction of NO
(down to 126 mg/Nm
(13%O
)) in a 15 kW pellet boiler upon the introduction of FGR. However, the authors also detected an increment of CO emissions, entailing the existence of a trade-off between the two pollutants.
In this article, the results of an experimental analysison a pellet stove tested with and without FGR are presented. The stove has a burning power of 7–9 kW. The work aims to experimentally demonstrate that the introduction of this relatively simple technology can considerably reduce the emission of pollutants in the atmosphere, making these products more environmentally friendly. The experimental investigation has been performed in the framework of a collaboration between the University of Brescia and AICO S.p.A., a pellet stove manufacturer, and it is a part of a project for the reduction of CO, PM and NO
emissions. The stove model used during the tests is indeed the result of an optimization process on the burner pot and the positions of air inlets presented in other publications of the authors [
9,
36]. This process led to a substantial reduction in CO, an appreciable reduction in PM, and a minor reduction in NO
. However, this NO
reduction was not sufficient to meet the requirements for the “5 stars” Italian quality label in
Table 1. Therefore, FGR was tested in this study to verify whether it could be a viable solution for low-power size wood pellet stoves to reduce NO
below the 100 mg/Nm
(13%O
) limit.
The rest of the paper is organized as follows:
Section 2 introduces the pellet stove under investigation. The experimental set-up and the test procedure are described in
Section 3.
Section 4 presents the results of the study, followed by a discussion. Conclusions are drawn in
Section 5.
2. Materials
The pellet stove used for the experimental tests was a “Ravelli Natural 7” model manufactured by AICO S.p.A., whose burning power range was 7 to 9 kW. This appliance was classified as airtight, i.e., when subjected to an overpressure of 50 Pa its leakage was less than 1.75 m
/h under normal conditions (temperature 0 °C, pressure 101.3 kPa). In this appliance, the fuel was fed into the combustion chamber through a screw/auger conveyor system, whose ON/OFF operation regulated the fuel flow. The flow rate of combustion air was adjusted by the speed of the flue gas extraction fan at the outlet of the stove. In its standard configuration, the stove was equipped with the “type A” burner pot described by Polonini et al. [
9] and patented by AICO S.p.A. [
37]. In the tests carried out for the present study, the stove has been equipped with a deeper burner pot, identified as “type B” [
9] and illustrated in
Figure 1. The use of this model of burner pot was previously found to be associated with lower CO and PM emissions if compared with traditional, less deep components [
9].
Two configurations of the pellet stove have been tested: without and with FGR, both shown in
Figure 2. In the tests with FGR, the standard stove model was modified as shown in
Figure 2 (right).
The stove was airtight. Therefore, with reference to
Figure 2, there were only one main inlet for combustion air (a) and one flue gases outlet (b). The air inflow was subdivided inside the stove into primary (c), secondary (d) and tertiary air flows (e). To prevent significant leakage between the inside and the outside of the stove, the pellet hopper (f) was isolated from the external environment. Primary and secondary inlets were separated by the burner pot geometry (
Figure 3). The tertiary inlet was separated from the others by a fork of the inlet duct, thus tertiary air entered the combustion chamber flame zone from the top.
A flue gas extractor fan regulated the excess air ratio, and during the tests it was set to maintain CO emissions as low as possible.
FGR is a technique that deviates a part of flue gases into the inlet air channel to generate a mixture of air and flue gases. As shown in
Figure 2 (right), a pipe in the tested stove, FGR channel (g), connected the flue gas outlet (b), downstream of the flue gas extractor (h), with the space around the burner pot, below the combustion chamber. The recirculating flue gas flow rate was not regulated, but resulted from the pressure difference between the outlet pipe and the chamber, due to the flue gas extractor. In the first attempts to introduce FGR in this stove, the flue gas outlet was directly connected to the air inlet pipe: mixing between the two gas streams started in the air inlet pipe, ahead of the chamber. Tests on this configuration were not satisfactory since no significant reduction of NO
was recorded. Then the configuration presented here was adopted. It was characterized by mixing developing in the chamber around the burner pot; therefore, the combustion mixture fed reactions through primary and secondary inlets only, while ambient fresh air fed the flame through the tertiary inlet.
As concerns fuel, the same ENPLUS A1 quality of pellets has been used in all tests. Mass fractions and lower heating value are specified in
Table 2.
3. Testing Procedure and Experimental Setup
The tests on the stove in either configuration required 5 days of experiments. All the tests performed during a single day of testing and in the same combustion conditions will be denoted here as a “test session”.
A regular day of testing started in the morning with the setting of operation parameters and stove ignition: the burner pot, in particular, was emptied of all the residuals from the previous day. In a range from 60 to 90 min from the ignition, the combustion reached quasi-steady condition which was detected upon monitoring flue gas temperature. At this point, several tests were performed: each test lasted 30 min and up to six tests were performed during a single test session. The operation parameters were kept fixed throughout a test session. At the end of the day, the pellet feeding was switched off and the combustion air flow rate was increased to quickly burn away the pellets left in the burner pot (extinguishing stage). This process lasted approximately 15 min.
For the measurement of burning rate , the whole stove was put on a platform scale according to the indications of the EN 16510-1:2018 standard (see also prEN 16510-2-6). The average burning rate was evaluated by dividing the stove weight decrement during the entire day of testing by its duration. Here, the duration is defined as the time interval from the beginning of the first test to the end of the last one.
Flue gases measurements and PM sampling were done in the measurement section, just downstream of the stove outlet. The flue gas draft was regulated by a mechanical aspiration system and was maintained constant at 8–10 Pa for all the combustion period. A scheme of the set-up is shown in
Figure 4.
During each test, O, CO, PM and NO were measured simultaneously and continuously. A gas analyzer ABB EL3020 equipped with electrochemical oxygen sensor was used to measure the concentration of O in dry gas in the form of volume percentage with an accuracy of ±0.2%. An ABB Uras26 infrared photometer mounted on the same analyzer was used to measure CO and NO fractions in parts-per-million, with an accuracy of ±2 ppm. Instantaneous PM emissions (PM) were measured with a TESTO 380 probe, with ±0.1 mg/Nm measurement resolution. For all these measures, the sampling time was 5 s, and the average over the 30 min test (360 samples) was calculated for each gas and for PM.
As well as measuring the instantaneous amount of particles during the test (PM), the total amount of particles in a 30 min test (PM) was measured by the filter-gravimetric method described in the CEN/TS 15883:2009 standard (see also prEN 16510-2-6). The particles were collected by a filter and weighed, then the total particle mass was divided by the amount of aspirated gas (measured by a Dr. Födisch GMD 12 gravimetric measuring device). The quartz fiber filter adopted in the tests had a retention efficiency of 99.998% of the particulate with 0.3 m diameter, while the analytical balance used to weigh the particles deposited on the filter was a Mettler-Toledo ME104, with ±0.08 mg measurement accuracy. According to the CEN/TS 15883:2009 standard (see also prEN 16510-2-6), the pump was set to extract flue gases at a constant flow rate of 10 L/min (accuracy ±2%).
A time lag between two consecutive tests was necessary to replace the filter and for the instrument self-adjustment. During these operations, the combustion conditions were kept fixed. Although the EN 14785:2006 and prEN 16510-2-6 standards prescribe to average O, CO, CO, and NO over three hours, here, the average values have been calculated over the 30 min in which the PM is collected by the filter.
4. Results and Discussion
The experimental results for the stove without FGR and with FGR are summarized in
Table 3 and
Table 4, respectively. Data were collected in 13 tests without FGR and in 11 tests with FGR. In test codes
-
d-
s,
is equal to S for tests without FGR and to R for tests with FGR,
n is the test progressive numbering,
d and
s stand for the testing day and test session, respectively.
To allow for a proper comparison of results, the average CO, PM
, PM
, and NO values collected during a test are normalized to the same concentration of 13% of O
. The CO fraction is multiplied by its density of 1.25 kg/Nm
, and NO fraction is multiplied by the density of NO
of 2.05 kg/Nm
according to the EN 16510-1:2018 standard (in this work, NO multiplied by the density of NO
is defined as NO
). Therefore, CO, PM
and PM
, and NO
results are presented in milligrams per normal cubic meter at 13% of O
. Indicating the average values with a bar over the symbol, the formulas used for unit normalization are:
where
is the mass of the filter before the measurement,
is the mass of the filter after the measurement, and
is the amount of aspirated gas during the measurement period. Similarly,
The burning power, that is, the chemical power available to the stove, is calculated with the equation
where
P is the burning power, LHV is the lower heating value in
Table 2 and
is the burning rate. The nominal power is obtained by multiplying the burning power
P by the thermal efficiency.
Finally, the thermal efficiency is calculated as prescribed in Sec. A.6.2.1 of EN 16510-1:2018 standard.
Tests in testing day no. 1 were grouped in three different sessions. The speed of the flue gas extraction fan was changed twice and was different for each of the three sessions. After each speed change, data collection was started only after reaching quasi-steady conditions as shown by the standard deviation of exhaust gas temperature during each test.
4.1. Effect of Recirculation on CO, PM and NO Emission Mean Values
In
Table 5, the mean values of O
content and emissions are summarized for the configurations without and with FGR, along with standard deviations. They are obtained by averaging the values reported in the corresponding columns of
Table 3 and
Table 4.
The experimental measurements illustrated in
Table 5 and
Figure 5 demonstrate that the application of FGR technology reduces the total amount of emissions.
In particular, CO emissions decreased by almost 80% and PM emissions by over 45%. Furthermore, an 11 % reduction in NO was observed.
4.2. Effect of Recirculation on CO, PM and NO Distribution vs. O Content
In this paragraph, the relations between emissions (CO, PM and NO
) and excess air, defined as the O
content in the flue gases, are analyzed. It is worth remarking that excess air in the flue gases does not depend only on the flue gas extractor velocity, but also on the instantaneous burning rate and instantaneous temperatures of the fire that continuously vary during the combustion. Moreover, the pellet mass falling in the pot also varies at each release from the conveyor system, depending on the number and total length of the grains released [
36]: hence, a wide O
variability can be expected even at fixed operation settings. To have a clear understanding of the trends despite data scattering, the instantaneous values of emissions have been synthesized in average values over narrow intervals of O
. It is worth specifying that all the 8640 data records collected in the 24 tests were used to draw
Figure 6,
Figure 7 and
Figure 8. A brief description of the procedure that was followed to obtain the average CO, PM and NO
distribution vs. O
content can be found in
Appendix A.
It is well known that CO emissions are influenced by excess air, specified by O
content in the flue gases; indeed, there is a specific percentage of O
that minimize CO emissions, as pointed out in several studies [
38,
39]. The experimental evidence in
Figure 6 shows that this percentage varies depending on the presence or the absence of a recirculation system: in the case without FGR, the lowest CO emissions were found at O
content between 8 and 9%, and their value was around 20 mg/Nm
(13%O
). On the other hand, when the FGR system was active, CO emissions attained very low values, below 5 mg/Nm
(13%O
), for a wider O
content interval, between 5 and 7%.
Furthermore, with FGR, CO emissions did not exceed 50 mg/Nm (13%O) over the entire range of excess air, whereas values well above 100 mg/Nm (13%O) could be observed without FGR at low and high O content values.
With regard to PM emissions, in
Figure 7, PM
measurements carried out with the TESTO 380 probe are plotted as a function of O
content in the flue gases. As in the case of CO emissions, PM emissions were particularly low for a specific interval of O
, which varied depending on the presence or absence of the recirculation technology: the “optimal” O
range was 5–7% in presence of FGR, and 8–9% without this technology. The minimum values of emissions in the two cases were about 6 and 11 mg/Nm
(13%O
), respectively, with the largest recirculation-driven improvement being obtained at low values of excess air.
As concerns the emissions of NO
, which are an unwanted product of combustion, non-correlated with CO emissions, it can be observed that their distribution vs. O
content had indeed a behavior different from those of CO or PM, as it tended to increase up to a maximum value and then plateau (
Figure 8). In addition, in this case there was a reduction of emissions associated with FGR, although slight. In particular, for percentages of O
below 6%, NO
emissions were lower than 100 mg/Nm
(13%O
), while, without FGR, NO
emissions were lower than 100 mg/Nm
(13%O
) only for very small O
percentages.
From the results plotted in
Figure 6,
Figure 7 and
Figure 8, it can be concluded that FGR does not influence the shape of the distribution of CO, PM, and NO
emissions vs. O
content. However, FGR shifts the distributions leftwards, i.e., towards lower values of O
and, at the same time, it decreases emissions at all O
values.
4.3. Final Remarks
The implementation of an FGR system in the stove has reduced pollutant emissions. The reduction is apparent considering both CO, PM, and NO
average values over several tests (
Figure 5) and their distribution vs. O
content in flue gases (
Figure 6,
Figure 7 and
Figure 8). The evaluation of the reduction significance will be based on the comparison with current emission limits enforced by Italian and European regulations, as summarized in
Table 1.
With regard to CO, Tschamber et al. [
40] and Labbé et al. [
41] have shown that the average CO emissions from wood pellet combustion can strongly change depending on the adopted stove model; in these articles, CO emissions varied from 50 to 850 mg/Nm
(13%O
). This interval extends well above the current limit of allowed emission which is 250 mg/Nm
(13%O
) (
Table 1). As mentioned in the introduction, the stove model used in this study was optimized to reduce CO and PM emissions. The CO emission levels of the optimized AICO’s burner pot are well below the 250 mg/Nm
(13%O
) limit: it can be observed that the average CO value in
Table 5 without FGR is 34 mg/Nm
(13%O
). Upon introduction of the FGR, CO emissions decreased by 80% to values around 7 mg/Nm
(13%O
): although the reduction is substantial, the implementation of an FGR system is not worth the cost since CO emissions are very low even without it.
With regard to PM, the emission values reported by Johansson et al. [
42,
43] and Schmidl et al. [
44] range between 12 and 80 mg/Nm
(13%O
), while, in the optimized stove model without recirculation presented in this article, the average PM emissions are around 12.3 mg/Nm
(13%O
) (measured using the filter-gravimetric method as required by the CEN/TS 15883:2009 and prEN 16510-26 standards). This value is below the strictest limit required by “5 stars” label (15 mg/Nm
(13%O
), see
Table 1); however, it is close to the limit. With FGR, the average emissions are reduced by a factor of 2, achieving 6.3 mg/Nm
(13%O
). Therefore, the adoption of an FGR system can guarantee a safe fulfillment of the requirement.
Nowadays, the most severe of the limits in
Table 1 for the current pellet stove technology is the 100 mg/Nm
(13%O
) on NO
emissions. As mentioned in
Section 1, among studies on fixed-bed combustors fired by biomass, only Archan et al. [
27] and Chen et al. [
34] report NO
emissions below 100 mg/Nm
(13%O
) upon use of FGR and air staging–in particular, between 85 and 90 mg/Nm
(13%O
). These values were obtained for 200 and 500 kW biomass boilers. The only study known to the authors characterized by a power rate comparable to that of pellet stoves is reported by Zandeckis et al. [
35]: here, the introduction of an FGR system in a 15 kW pellet boiler led to a reduction in NO
, but from 142 to 126 mg/Nm
(13%O
), i.e., still above the 100 mg/Nm
(13%O
) limit.
In this work, the adoption of FGR in a 7–9 kW pellet stove has reduced NO emission by slightly more than 10%. Compared to CO and PM reductions, it may not seem significant; however, it is quite an important result in that the emissions were reduced from 113 to 100 mg/Nm (13%O)—that is, they were lowered at or just below the threshold for the “5 stars” requirement of 100 mg/Nm (13%O). The implementation of an FGR system coupled with an optimized burner pot seems a feasible solution to develop an environmentally friendly pellet stove.
As an ending remark, in the studies by Archan et al. [
27] and Chen et al. [
34], the NO
emission reduction was improved upon control of the flue gas flow rate mixed with the combustion air flow. On the other hand, in the present study, mixing was not regulated and was governed by the pressure difference between the flue gases outlet pipe and the combustion chamber. In this respect, this study has to be considered preliminary. In future developments, a measurement campaign should be set up to investigate the optimal amount of recirculated gas that minimizes emissions without compromising combustion, and to further reduce NO
emissions to safely fulfill the 100 mg/Nm
(13%O
) limit.