Energy Minimization in Piperazine Promoted MDEA-Based CO2 Capture Process
Abstract
:1. Introduction
2. Methodology
2.1. Process Description
2.2. Model Development
2.3. Rich Vapor Compression Process (RVC) with Cold Solvent Split (CSS)
2.4. Total Equivalent Work and Cost of the Main Equipment
3. Results and Discussion
3.1. Parameter Sensitivity Study
3.1.1. Stripper Pressure Effect
3.1.2. MDEA/PZ Ratio Effect
3.2. Process Modification
3.2.1. Effect of Rich Vapor Compression Process (RVC)
3.2.2. Effect of Cold Solvent Split Process (CSS)
3.2.3. Effects of Combined RVC and CSS Processes
3.3. Comparison with MEA-Based RVC and Lean Vapor Compression (LVC) Processes
3.4. Direct Cost of Main Equipment and Annual Cost Saving
4. Conclusions
- Among different MDEA/PZ concentration ratios (45/5, 40/10, 35/15, and 30/20 wt.%), from an energy minimization point of view, 35/15 wt.% was selected to be an appropriate ratio. Although the energy requirement at 15 wt.% PZ was slightly higher than at 20 wt.%, PZ losses from the absorber were also higher (257 ppm) at 20 wt.% than at 15 wt.% PZ (172 ppm). The reboiler duty of 3.235 MJ/kg CO2 was obtained at a MDEA/PZ ratio of 35/15 wt.%. A stripper pressure of 2.3 bar was selected because above that pressure, the reboiler temperature was increased from 125 °C.
- In only the RVC process, the lowest total equivalent energy (among other P1 pressure) of 0.7 MJe/kg CO2 was obtained at 1.3 bar P1 pressure, which was 6.4% lower than the reference case. Similarly, a split fraction of 15% was chosen for the CSS process. The lowest reboiler duty of 2.78 MJ/kg CO2 was achieved at 15% split, and it was 14% lower than the reference case.
- In the combined RVC and CSS process, 1.5 bar P1 pressure and 15% split fraction were appropriate values. The total equivalent work was 0.627 MJe/kg CO2, the reboiler duty was 2.44 MJ/kg CO2, and the condenser duty was 0.33 MJ/kg CO2. The reboiler duty was reduced about 24.6% and the total equivalent work about 16.2% as compared to the reference case. The reboiler duty was reduced further, but due to the increasing of compressor power, the total equivalent work was also raised. The annual depreciation change was calculated as 1.22 M$/yr for the RVC with CSS process. The total energy cost saving was 1.79 M$/yr, and when considering the equipment cost, the total cost saving in one year was 0.67 M$.
Author Contributions
Funding
Acknowledgments
Conflicts of Interest
References
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Flow Rate (t/h) | Pressure (MPa) | Temperature (°C) | Mole Fraction (%) | ||
---|---|---|---|---|---|
CO2 | N2 | H2O | |||
775 | 0.11 | 40 | 12 | 78 | 10 |
Simulation Parameters | Values |
---|---|
Absorber pressure (bar) | 1.1 |
Absorbent flow rate (t/h) | 3500 |
Absorbent temperature (°C) | 40 |
MDEA/PZ concentration (wt.%) | 45/5 |
Heat exchanger LMTD (°C) | 10 |
Stripper pressure (bar) | 2.1 |
Reboiler temperature (°C) | 124.97 |
Pressure in P1 (bar) | Heat Exchanger MWTh | Vapors Fraction (mol.%) | Compressor Work (MWe) | Pumps (MWe) | Condenser Duty (MWTh) | Reboiler Duty (MWTh) | Total Equivalent Work (MJ/kg CO2) |
---|---|---|---|---|---|---|---|
1.1 | 165.4 | 6.56 | 5.056 | 0.121 | 0.299 | 68.73 | 0.653 |
1.3 | 163.0 | 5.50 | 3.242 | 0.121 | 0.316 | 73.54 | 0.631 |
1.5 | 159.9 | 4.56 | 1.993 | 0.121 | 0.331 | 78.34 | 0.626 |
1.7 | 157.3 | 3.80 | 1.160 | 0.121 | 0.343 | 82.23 | 0.628 |
1.9 | 154.4 | 3.13 | 0.599 | 0.121 | 0.352 | 85.92 | 0.637 |
2.1 | 151.7 | 2.58 | 0.232 | 0.121 | 0.358 | 89.22 | 0.645 |
Simulation Conditions | Reference Case (Optimal Conditions) | Cold Solvent Split | Rich Vapor Compression | Combined Process |
---|---|---|---|---|
Absorbent flow rate (t/h) | 3500 | 3500 | 3500 | 3500 |
Flue gas flow rate (t/h) | 775 | 775 | 775 | 775 |
L/G (mass) | 4.52 | 4.52 | 4.52 | 4.52 |
Lean CO2 loading (mol/mol) | 0.18 | 0.18 | 0.18 | 0.18 |
Split fraction (%) | -- | 15 | -- | 15 |
Results | ||||
CO2 mole purity (%) | 99 | 99 | 99 | 99 |
Compressor power (MW) | -- | -- | 2.57 | 1.99 |
Reflux ratio (mass) | 0.325 | 0.082 | 0.256 | 0.106 |
Condenser temperature (°C) | 20 | 20 | 20 | 20 |
Condenser duty (MJ/kg CO2) | 0.92 | 0.26 | 0.73 | 0.33 |
Reboiler duty (MJ/kg CO2) | 3.235 | 2.78 | 2.68 | 2.44 |
Total Equivalent work (MJe/kg CO2) | 0.7478 | 0.643 | 0.7 | 0.627 |
Total equivalent energy saving (%) | -- | 14 | 6.4 | 16.2 |
Processes | Reboiler Duty b (MJe/kg CO2) | Compressor Work c (MJe/kg CO2) | Pumps Work c (MJe/kg CO2) | Total Work (MJe/kg CO2) | Total Energy Saving (%) |
---|---|---|---|---|---|
Reference (this study) | 0.744 | - | 0.0038 | 0.7478 | - |
RVC (this study) | 0.616 | 0.08 | 0.0038 | 0.7 | 6.4 |
RVC + CSS (this study) | 0.561 | 0.0626 | 0.0038 | 0.627 | 16.2 |
Base a [20] | 0.813 | 0.068 | 0.881 | - | |
RVC + CSS [20] | 0.652 | 0.087 | 0.068 | 0.807 | 8.4 |
LVC + CSS [20] | 0.692 | 0.092 | 0.068 | 0.852 | 3.3 |
Parameter | Value |
---|---|
Installation factor | 4 |
Compressor lifetime | 10 |
Flash vessel lifetime | 25 |
Heat exchangers lifetime | 20 |
Electricity ($/MWh) | 67.5 [22] |
Annual plant operation time (h) | 7450 |
Equipment Cost (M$) | Base | RVC+CSS |
---|---|---|
Heat exchanger | 3.398 | 3.385 |
Compressor | - | 2.67 |
Reboiler | 0.68 | 0.594 |
Flash vessel | - | 0.541 |
Condenser | 0.232 | 0.166 |
Purchase cost changes | 3.05 | |
Annual depreciation change (M$/yr) | 1.122 | |
Energy cost saving | 1.791 | |
Total cost saving | 0.67 |
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Khan, B.A.; Ullah, A.; Saleem, M.W.; Khan, A.N.; Faiq, M.; Haris, M. Energy Minimization in Piperazine Promoted MDEA-Based CO2 Capture Process. Sustainability 2020, 12, 8524. https://doi.org/10.3390/su12208524
Khan BA, Ullah A, Saleem MW, Khan AN, Faiq M, Haris M. Energy Minimization in Piperazine Promoted MDEA-Based CO2 Capture Process. Sustainability. 2020; 12(20):8524. https://doi.org/10.3390/su12208524
Chicago/Turabian StyleKhan, Bilal Alam, Asad Ullah, Muhammad Wajid Saleem, Abdullah Nawaz Khan, Muhammad Faiq, and Mir Haris. 2020. "Energy Minimization in Piperazine Promoted MDEA-Based CO2 Capture Process" Sustainability 12, no. 20: 8524. https://doi.org/10.3390/su12208524
APA StyleKhan, B. A., Ullah, A., Saleem, M. W., Khan, A. N., Faiq, M., & Haris, M. (2020). Energy Minimization in Piperazine Promoted MDEA-Based CO2 Capture Process. Sustainability, 12(20), 8524. https://doi.org/10.3390/su12208524