1. Introduction
Horizontal well drilling technology can be traced back to 1927, and it was first put into practice in the 1940s [
1,
2]. In the 1950s and 1960s, it experienced a small upsurge of development and then stopped. In the 1970s and 1980s, with the rise in oil prices, an improvement in drilling matching technology, horizontal well development technology, and horizontal well technology was widely seen in the United States, Canada, and France. Nowadays, almost all types of reservoirs, such as depleted reservoirs, tight gas reservoirs, low-permeability reservoirs, marginal reservoirs, and high-permeability reservoirs, can be developed using horizontal well technology. In tight low-permeability reservoirs, natural fractures act as the only oil flow channel. The advantages of horizontal wells are particularly obvious. More than 70% of the horizontal wells drilled in the mid-1990s were completed in such reservoirs [
3,
4,
5]. The study of horizontal well reservoir fracturing stimulation technology began in the 1980s. Since the long horizontal section of horizontal wells often crosses the reservoir, it is difficult to achieve effective reservoir reconstruction by acidizing and fracturing the whole well section. Therefore, it is necessary to conduct fracturings in multiple sections to form ideal independent artificial fractures and maximize the technical advantages of horizontal wells in developing low-permeability oilfields. Compared to general fracturing of vertical wells and horizontal wells, staged fracturing can effectively induce reservoir fractures, increase the discharge area, and greatly improve the production of oil and gas wells [
6,
7,
8]. In recent years, with the continuous expansion of shale gas, tight oil/gas, and coalbed methane, horizontal well technology has been developed on an unprecedented scale, and new horizontal well fracturing technologies have been emerging [
9,
10,
11,
12,
13,
14,
15,
16].
One-trip multi-stage fracturing completion is a comprehensive method performed in open-hole horizontal wells. It combines the completion string and fracturing string as a one-trip string and runs down together. Tools run down the well, including bidirectional anchoring hangers, expandable open-hole packers, dropping ball promotion sliding sleeves, and differential pressure opening sleeves. Open-hole packers seal the horizontal section to achieve isolation from the fracturing operation part. In this way, the whole horizontal section can be completely fractured. By 2013, 21 fractured sections in one well had been achieved in the Changqing Oilfield in China, in which tight gas accounts for 70~80% of the total gas [
17]. Multi-stage acidizing technology and fracturing technology are commonly used in low-permeability reservoirs [
18].
The open-hole staged fracturing completion of horizontal wells involves a long horizontal open-hole section and a number of large-diameter tools. During the construction process, it is difficult to ensure that the completion string can be smoothly run to the specific position, and this is the key to successful fracturing completion [
19]. For example, one staged fracturing string stuck to the wellbore while being run down the well, and eight packers were set locally [
20]. This forced the researchers to change the fracturing stage from six to three. The actual length of the horizontal section was 1169 m, while the string only entered at 439 m, with a 730 m loss.
The running resistance of the string comes from two aspects: one is the axial resistance or rotation moment caused by friction after the string comes into contact with the wellbore, and the other is the local resistance caused by the string itself or wellbore conditions. In 2020, Guo and Rashid proposed an analytical model for axial force transfer in extended-reach drilling [
21]. Generally, friction refers to prior circumstances, so the model is established mainly based on the previous one developed in this work. The local blocking force is considered empirically according to the carrying capacity of rigid tools.
The investigation shows that although there is some theoretical analysis of the friction resistance of complex completion strings in horizontal wells, and the field has rich operation experience, accidents occur from time to time when the string cannot be run down to the bottom of the well. Such accidents are fatal, often leading to the abandonment of wells and huge economic losses. Running a completion string is a systematic operation, and even commercial software, such as Landmark, cannot predict the probability of resistance. Therefore, according to the field construction process, developing a new calculation method for pipe string axial force is necessary.
3. Results
3.1. Basic Data
Based on the data of well S from the Halfaya Oilfield in Iraq, the mechanical analysis is carried out.
Wellbore parameters: the well depth is 3737 m; the kick-off point depth is 2234 m; the production casing outer diameter is 177.8 mm, the wall thickness is 10.36 mm, the running depth is 2926 m, and the well deviation is 90°. the open hole horizontal section is from 2926 m to 3737 m with a diameter of 152.4 mm.
A drill pipe and heavy-weight (HW) drill pipe are used to send and release the completion casing string. The string has eight open-hole packers, and the distance from the packers to the string toe section is 90 m, 150 m, 235 m, 340 m, 475 m, 580 m, 684 m, and 760 m, respectively.
The top of the casing is the hanger packer, and above the hanger packer is the drill pipe and heavy-weight drill pipe. The main parameters of the overall string are shown in
Table 1. The friction factor is 0.25 in the casing and 0.3 in the open hole.
3.2. String Axial Force
From previous models and parameters, the hook load is calculated along the depth, which is shown in
Figure 4. It can be seen that the hook load has the following characteristics:
- (1)
The hook load difference between running down and pulling up gradually becomes larger when the string passes the kick-off point;
- (2)
During the pulling-up process, the hook load increases with the string length;
- (3)
During the running-down process, the hook load increases monotonously before the string enters the horizontal section, and decreases slowly after entering the horizontal section.
When the string reaches the bottom, the axial force distribution is shown in
Figure 5. It can be seen that the maximum axial compressive force occurs around 2700–2800 m, about 50 kN. However, this section is curved, and the string will not be subject to spiral buckling. In the horizontal section, the axial compressive force decreases to about 40 kN. For the 4-1/2” casing, the critical value of spiral buckling is about 220 kN in horizontal wells. Therefore, the string will not buckle.
3.3. Effect of Local Resistance Amplification
It is assumed that the completion string of well S has been run to the bottom. In order to investigate the relationship between the local resistance and the hook load, it is assumed that the string encounters axial resistance of 0 kN, 50 kN, and 100 kN near its bottom. The corresponding hook load variation is shown in
Table 2.
In this table, the hook load increases during the pulling-up process, and the hook load decreases during the running-down process when compared to the case of no local resistance. The amplification factor is the ratio of the increase and decrease value to the local resistance value.
The following main features can be obtained:
- (1)
The resistance at the string bottom is amplified during the upward transmission process;
- (2)
The amplification factor of the pulling-up process is greater than that of the running-down process;
- (3)
The larger the local resistance, the larger the amplification factor.
Figure 6 shows the hook load differences between the pull-up process and run-down process under different
Fs conditions. As can be seen,
Fs = 0 kN means that there is no blocking in the well, and that the calculated hook load is 705.33 kN. If the blocking point resistance is 50 kN, the hook load will be increased by 77.74 kN instead of 50 kN. And if the blocking point resistance is 100 kN, the hook load will be increased by 158.58 kN instead of 100 kN. According to the relationship between the blocking point resistance and the hook load, the amplification factor can be obtained.
To study the influence of blocking position on hook load, several blocking point locations were assumed. For Case 1, in which assumes that the blocking point is located in the middle of the kick-off segment and with a depth of 2580 m (1156 m away from the bottom), the corresponding hook load variation is shown in
Table 3.
For Case 2, in which assumed that the blocking point is located at the beginning of the kick-off segment and with a depth of 2230 m (1506 m away from the bottom), the corresponding hook load variation is shown in
Table 4.
Table 5 shows the amplification factor changes under different blocking situations. Also, the amplification factor with two blocking point situations is calculated.
The calculation results showed that:
- (1)
The amplification factor increases as the distance of blocking point from the bottom hole increases;
- (2)
The amplification factor is affected by the resistance value, position, and other factors;
- (3)
The axial resistances at different positions have mutual amplification and accumulation effects;
- (4)
The variation of the hook load caused by two resistances is greater than the sum of hook load variations caused by a single resistance.
4. Discussion
4.1. Hook Load Comparison
The open-hole completion string of this well is equipped with eight external packers, and the running process is smooth. After the string runs into the hole, the hook load of the pull-up and run-down processes are recorded, as shown in
Table 6. At the same time, the predicted hook load before the operation is given in the table.
When the string is running down, the hook load relative difference is −2.55%, which means that the running operation of the completion string is smooth, and thtt the quality of the well is good. There are no obvious shoulders, no diameter shrinkage, no collapse, and the hole is clean. Furthermore, the design and use of completion mud, wiper trip technology, and completion string are reasonable.
When the string is pulling up, the hook load difference is 6.53%, which indicates the completion string encounters additional resistance; compared to the run-down relative difference, it is shown that the pull-up process will encounter a larger resistance.
During the in-site process of string pull-up and run-down, some of the parameters cannot be accurately obtained, such as the fineness of the wellbore description and the controllability of the construction equipment. Therefore, from the industrial analysis perspective, there will be errors between the recorded data and theoretical analysis results.
4.2. Error Analysis and Resistance Source Judgment
Based on the in-site pigging data (4″ drill pipe and 4″ heavy weight drill pipe, with 1.23 g/cm
3 mud density). The well string load limit conditions are 770 kN during pull-up, and 510 kN during run-down, and the calculated friction factors are shown in
Table 7.
The maximum error and average error of the axial force during the pull-up process are −5.21% and −0.40%, respectively. The maximum error and average error of axial force during the run-down process are −2.10% and 0.05%, respectively. All the relative errors between calculated results and in-site limited values are within the range of 10%, which indicates that the calculated values are reliable.
The calculated friction factor is applied to the drilling operation of the double-pigging process and the operation of the completion string. The error between the calculated value and the in-site recorded value is small, indicating that the stability of the mud system is good, which will ensure the smooth running of the completion strings with multiple external packers in the Sadi horizontal wells of Halfaya Oilfield.
The work results were successfully applied and verified, providing a successful experience for the future completion design and construction. Combined with calculation results and analysis, the following experience and guidance are provided:
- (1)
Use the parameters recorded during drilling to obtain the friction factor of pipe string in the wellbore. Verify it through the pigging string to ensure that the value is reasonable, and then apply it to the friction analysis of the string running operation.
- (2)
There is an error between the recorded value and the calculated value of the completion string load. Since the completion string cannot be rotated, the specific source of resistance cannot be confirmed, which highlights the importance of the early mud system and well drilling plan. At the same time, it also shows that after the external packer is installed, there is still room for improvement in the calculation of the pulling-up and run-down resistance.
In general, error sources also include the following parts:
- (1)
In the kick-off section, the contact force between the string and the wellbore is relatively high, which makes it more difficult to conduct the pipe string operation. At the same time, it is difficult to guarantee the smoothness of the curved well section, and the fine description of the whole process is even more difficult.
- (2)
In the target well interval, the wellbore’s geometry may be down-dipped, horizontal, up-dipped, or even wavy shape. When the target section is down-dipped, it is more difficult to pull the pipe string up than it is to run the string down. Meanwhile, various factors lead to differences in the wellbore cleanliness, which will affect the calculation accuracy.
- (3)
The pipe string structure, such as the completion pipe strings, is equipped with multiple packers, centralizers, and other tools. On the one hand, it changes the bending stiffness of pipe string, and on the other hand, it is also extremely sensitive to micro-steps and cuttings beds on the wellbore.
- (4)
Rotary run-down casing, floating run-down casing, and other processes can reduce friction while increasing the difficulty of calculating accuracy.
5. Conclusions
The proposed model focuses on dealing with multiple resistances of different points of the completion string. This model makes up for the technical defect of some common software, such as Landmark. It is suitable for the simulation of the casing running process with multiple external packers. Through the change in hook load, blocking position, and resistance character, the resistance value can be estimated more accurately.
Based on the case study of a horizontal open hole completion string from the low permeability Sadi reservoir of Halfaya Oilfield, Iraq, the following conclusions are obtained:
The string resistance at the horizontal section will be amplified during the pulling-up process;
The amplification factor is larger during the pulling-up process than during the running-down process;
The larger the local resistance, the larger the amplification factor;
The amplification factor is affected by resistance value, position, and other factors;
The axial resistances at different positions have mutual amplification and accumulation effects;
The change in hook load caused by both resistances is greater than the sum of hook load changes caused by a single resistance.